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等级: 二袋长老
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Reference BSD: CH10.2, CH10.7 The pulse detection time has fallen below the specified time range. Check items ・ Check the EXIT MOTION SENSOR (PL 5.3) for improper installation, contamination, and foreign substances. ・ Check the SENSOR WHEEL (PL 5.3) of the EXIT MOTION SENSOR for damage, contamination, and revolution failure. ・ Check the paper transport path for anything that might obstruct the paper. ・ Check the PRESSURE ROLL (PL 5.4) and the HEAT ROLL (PL 5.2) for contamination, wear, and revolution failure. ・ Check the GEAR (PL 5.1) and etc. for disengagement and damage. ・ Check the EXIT ROLLER (PL 5.4) for contamination, wear, and revolution failure. ・ Check the GEAR (PL 5.4) and etc. for disengagement and damage. ・ Check whether an out of spec paper is being used. Procedure Enter IOT DC330[010-207]. Remove the SENSOR WHEEL of the EXIT MOTION SENSOR and remove any obstruction on the sensor light path. Use a sheet of blank paper to block/clear the light path to the sensor. Does the display of IOT DC330[010-207] change between High/Low? Y N Go to the Permeable Sensor Failure FIP and check the EXIT MOTION SENSOR (PL 5.3). Install the SENSOR WHEEL of the EXIT MOTION SENSOR. Switch the combination of the IOT DC330[010-081~084] output signals (Bit0, Bit1, Bit2, Bit3). (Refer to [Chapter 7 BSD CH10.2]). Enter IOT DC330[010-080] and turn it ON. Does the FUSER DRIVE MOTOR rotate? Y N Go to 010-324 Fuser Drive Motor Lock Error FIP. Replace the IOT PWB (PL 7.1). |
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